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	<title>FastAlley &#187; Projects</title>
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	<description>Sailing Adventures</description>
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		<title>2010 JULY &#8211; Weather Station</title>
		<link>http://fastalley.com/2010/07/21/2010-july-weather-station/</link>
		<comments>http://fastalley.com/2010/07/21/2010-july-weather-station/#comments</comments>
		<pubDate>Thu, 22 Jul 2010 00:08:32 +0000</pubDate>
		<dc:creator>admin</dc:creator>
				<category><![CDATA[Projects]]></category>
		<category><![CDATA[Fastalley]]></category>
		<category><![CDATA[Julia Brown]]></category>
		<category><![CDATA[trimaran]]></category>

		<guid isPermaLink="false">http://fastalley.com/?p=567</guid>
		<description><![CDATA[2010 JULY &#8211; Weather Station I have a West Marine model Weather Base 20 which works perfectly well and tells the temperature, humidity, time, and most important to me as a sailor, it tells the wind speed and wind direction.  That is, it did until one of the 3 cups on the external wind indicator [...]]]></description>
			<content:encoded><![CDATA[<p><strong>2010 JULY &#8211; Weather Station</strong></p>
<div id="attachment_568" class="wp-caption aligncenter" style="width: 310px"><img class="size-thumbnail wp-image-568" title="DSC02551" src="http://fastalley.com/wp-content/uploads/2010/07/DSC02551-300x150.jpg" alt="Weather monitor - wind indicator" width="300" height="150" /><p class="wp-caption-text">Weather monitor - wind indicator</p></div>
<p>I have a West Marine model Weather Base 20 which works perfectly well and tells the temperature, humidity, time, and most important to me as a sailor, it tells the wind speed and wind direction.  That is, it did until one of the 3 cups on the external wind indicator broke off.  With only 2 cups left they balanced each other out and the monitor no longer spun/rotated in the wind – so I no longer got the wind speed.</p>
<p>I thought I would be able to dismantle the wind indicator, remove the offending piece, and replace it with a new piece with the requisite 3 cups.  The weather base is made by West Marine so off I went to WM to buy a replacement part.  I entered the WM store and headed straight for an assistant at the counter.</p>
<p>I explained my problem and the assistant looked dubious.  He said he thought that WM sold the entire base as one unit and that spare parts were not available.</p>
<p>At this time the gentleman standing next to me piped up helpfully.  Why not just stick a bottle cap in the place of the missing cup and it will work just fine, he offered.  And Coca Cola caps work perfectly, he added.</p>
<p>The mere thought of an ugly Coke cap glued onto any part of  my beautiful boat was about as attractive as a boil on a baby’s bottom.  I turned and gave the man a withering “You stay out of this!” glare.  He shrugged.</p>
<p>The attendant and I went thru the WM catalog.  Turns out that WM no longer makes that particular model, however, for just $549 I can buy a whole new latest-and-greatest weather base.  Excluding the cost of an electrician to remove the old weather station and fit the newest contraption, of course..</p>
<p>There are a lot of things I need for the boat right now, and a new weather base is not one of them, so I left the store.</p>
<p>Once I got back to the boat I studied the non-spinning wind indicator and pondered the problem.  The more I thought about the man’s suggestion of a Coke bottle cap, the more it made sense.  Eventually I decided it was worth a try, especially since the stupid indicator was not working anyway&#8230;  And there are no spare parts for it&#8230;  And I didn’t feel like buying a new one.</p>
<p>So off I went to the store and bought a 6-pack of Cokes.  I noticed that the bottle caps are a bright red so I decided to paint them black.  I picked up a cheap bottle of nail polish – black nail polish like people use on Halloween to enhance their witch costumes.</p>
<p>Then back to the boat.  Over the weekend I drank the cokes and kept the lids which I painted black.  Then I mixed up a batch of marine glue, climbed up on the roof of the dodger, leaned over the davits precariously, and glued a now-black cup in the spot of the missing cup.  I waited expectantly for the indicator to start spinning happily in the 10-knot wind but it just sat there.</p>
<div id="attachment_569" class="wp-caption aligncenter" style="width: 310px"><img class="size-thumbnail wp-image-569" title="DSC02552" src="http://fastalley.com/wp-content/uploads/2010/07/DSC02552-300x150.jpg" alt="Its the little fella below the big wind generator" width="300" height="150" /><p class="wp-caption-text">Its the little fella below the big wind generator</p></div>
<p>I sat and watched the movement of the indicator – or non.movement in this case &#8211; and it seemed that since the other 2 cups were on extended arms and my Coke cup was glued straight to the mounting base, it was preventing a rotation from starting.  If I knocked it with my hand then it spun away and continued to spin, but once I stopped it again, it couldn’t restart its spin.  Obviously I must have slept thru the lesson about wind dynamics in school.</p>
<p>So I thought if I glued another 2 cups to the mounting then the new 3 cups would generate the start speed needed to get it spinning.  So I did that.  Now I had 5 cups on the indicator – 3 Coke caps (painted Halloween black) glued directly to the monitor, and 2 originals on their extended arms.</p>
<p>By this time the wind had picked up so I sat back waiting for the <em>vroooom</em> that would indicate my monitor was spinning wildly &#8211; but it didn’t move.  All I had done was counter balance the stupid thing again.  As I watched, the wind would catch the cup on the extended arm and shove it clockwise.  Then the wind would catch the other extended cup and shove it anti-clockwise.  So the indicator wobbled back and forth, but did not fully rotate.</p>
<p>Obviously I needed to replace a-cup-on-an-extended-arm like the one that broke off.  I know, I know, I shouldn’t have second guessed the original designer – but who knew 5 cups would not do the trick?!</p>
<p>Back to the drawing board….  I cut up an expired credit card into thin strips to use as the arm extension and glued the strips together to get rigidity.  And painted it black.  Then I glued the (4<sup>th</sup>) cup to the extension, and glued the extension in the missing place on the indicator.</p>
<div id="attachment_574" class="wp-caption aligncenter" style="width: 310px"><img class="size-thumbnail wp-image-574" title="DSC02553" src="http://fastalley.com/wp-content/uploads/2010/07/DSC025532-300x150.jpg" alt="Okay, it says zero now - but the wind wasnt blowing when I took this pic" width="300" height="150" /><p class="wp-caption-text">Okay, it says zero now - but the wind wasnt blowing when I took this pic</p></div>
<div class="mceTemp">The thing started spinning madly – at last.  I bolted downstairs and my weather base showed the wind at 14 knots.  Oh joy!</div>
<p>So now instead of a neat wind indicator on my davit with 3 neat cups on extensions, now I have the thing bristling with Coke bottle caps &#8211; all painted Halloween black.</p>
<p>The next time someone comes up with a simple fix to an expensive problem, I hope I have the good sense to ask some in-depth questions instead of dishing out a snotty look.  To the man in WM that received The Look, I humbly apologize.</p>
<p><span style="color: #0000ff;">Cost to replace:                    Newest weather base $549         + handyman electrician at $65 p/hr</span></p>
<p><span style="color: #0000ff;">Cost to fix: </span></p>
<p><span style="color: #0000ff;">6-pack of Cokes           $2.99</span></p>
<p><span style="color: #0000ff;"> 1 black nail polish      $1.99</span></p>
<p><span style="color: #0000ff;"> TOTAL =       $5  (I already had the marine glue)</span></p>
<p><span style="color: #0000ff;"> </span></p>
<div id="attachment_575" class="wp-caption aligncenter" style="width: 310px"><img class="size-thumbnail wp-image-575" title="DSC02554" src="http://fastalley.com/wp-content/uploads/2010/07/DSC02554-300x150.jpg" alt="The weather station on my Navigation station" width="300" height="150" /><p class="wp-caption-text">The weather station on my Navigation station</p></div>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
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		<title>APRIL 2010 &#8211; BATTERIES &amp; ELECTRICAL SYSTEM</title>
		<link>http://fastalley.com/2010/06/13/april-2010-batteries-electrical-system/</link>
		<comments>http://fastalley.com/2010/06/13/april-2010-batteries-electrical-system/#comments</comments>
		<pubDate>Sun, 13 Jun 2010 16:31:43 +0000</pubDate>
		<dc:creator>admin</dc:creator>
				<category><![CDATA[Projects]]></category>
		<category><![CDATA[Fastalley]]></category>
		<category><![CDATA[Julia]]></category>
		<category><![CDATA[trimaran]]></category>

		<guid isPermaLink="false">http://fastalley.com/?p=510</guid>
		<description><![CDATA[Nav station board     APRIL 2010 &#8211; BATTERIES &#38; ELECTRICAL SYSTEM House bank batteries replaced Engine starter battery replaced Battery charger replaced Shunt repositioned “Amps in” dial replaced   When my boat was in Long Beach I took the boat out regularly and gave the engine a run under load, but this year I [...]]]></description>
			<content:encoded><![CDATA[<div class="mceTemp" style="text-align: left;">
<dl id="attachment_512" class="wp-caption  alignnone" style="width: 436px;">
<dt class="wp-caption-dt"><img class="size-thumbnail wp-image-512" title="Nav station board" src="http://fastalley.com/wp-content/uploads/2010/06/DSC02479-300x150.jpg" alt="Nav station board" width="426" height="254" /></dt>
<dd class="wp-caption-dd">Nav station board</dd>
</dl>
</div>
<div class="mceTemp mceIEcenter" style="text-align: left;">
<p> </p>
<p> </p>
<p><strong>APRIL 2010 &#8211; BATTERIES &amp; ELECTRICAL SYSTEM</strong></p>
<ul>
<li>House bank batteries replaced</li>
<li>Engine starter battery replaced</li>
<li>Battery charger replaced</li>
<li>Shunt repositioned</li>
<li>“Amps in” dial replaced</li>
</ul>
<p> </p>
<p>When my boat was in Long Beach I took the boat out regularly and gave the engine a run under load, but this year I am up in the San Francisco Bay and the winters are wet, wet, wet so I found that I simply never walked thru the rain to the boat.  It just sat there at the dock, neglected and forlorn.</p>
<p> And it rained.  And rained.  And rained.  For months.  And months.  And months.</p>
<p> It April now and after the sun broke thru quite suddenly and brightly and I was off to the boat again.  I tried to fire up the engine but no joy.  I checked both battery banks, the house bank and the starter battery, and they looked charged according to my reading of the dials (I could be wrong), so I tried again to start the engine.  And again, nothing.  I tried cross-connecting the house and starter batteries with the combined effect of zero.  I shut the boat up and trudged back up the dock to my car.</p>
<p>The next time the weather cleared I met an electrician out at FastAlley.  He went over the electrical board, examined the batteries, checked the battery charger &#8211; and declared the whole lot dead.  The battery charger had failed and taken out the house set.  Or, he said, one of the batteries had shorted and blown the rest of the batteries as well as the charger.  Who knows.  All I did know for sure was that all 4 house batteries were fried, as well as the battery charger.</p>
<p>The 4 (dead) batteries in the boat are about $400+ each, which made me unhappy, however, I felt better when Duane said that the batteries were from 2003 and long past their useful life, and should be replaced anyway.  He said the life of a battery is at most 5 to 6 years so I had had good use out of them.  That only lessened the $-pain a little.</p>
<p>He asked when I was going cruising?  I said, Probably in 2 years.  He said that I really don’t need 4 deep cycle gel batteries while I am tied up to the dock and using shore power, and suggested that I buy just 2 house batteries, and a good engine starter battery.</p>
<p> </p>
<div id="attachment_511" class="wp-caption aligncenter" style="width: 310px"><img class="size-thumbnail wp-image-511" title="New battery charger &amp; shunt moved" src="http://fastalley.com/wp-content/uploads/2010/06/DSC02478-300x150.jpg" alt="New battery charger &amp; shunt moved" width="300" height="150" /><p class="wp-caption-text">New battery charger &amp; shunt moved</p></div>
<p>Yesterday we met at the boat, with the 3 batteries, installed them, and turned on the engine.  It groaned and coughed and then started.  What a wonderful sound – I feel so lost when my engine won’t run because I won’t sail in or out of a slip in the trimaran.  I did that in my little 22ft Catalina but I won’t do that in this wide-bodied monster. </p>
<p> </p>
<p>I ran the engine for about 45 minutes to fully charge the batteries.</p>
<p> </p>
<p><strong><span style="color: #0000ff;">Replacement $cost – the battery charger, batteries, shunt, dial</span></strong><strong><span style="color: #0000ff;"> </span></strong></p>
<p><span style="color: #0000ff;">AC Charger, Xantrex TrueCharge,                        $280</span></p>
<p><span style="color: #0000ff;">1 EA Battery, 12V, Flooded, Group 24               $135</span></p>
<p><span style="color: #0000ff;">2 EA Battery, 12V, Flooded, Group 24              $216</span></p>
<p><span style="color: #0000ff;">Troubleshoot problems                                          $195</span></p>
<p><span style="color: #0000ff;">Replace charger+batteries                                    $130</span></p>
<p><span style="color: #0000ff;"><strong><em>Total, parts and labor</em></strong><strong>                                   $1,015</strong></span></p>
<p><span style="color: #0000ff;">Still to do                                                                   $&#8212;&#8212;</span></p>
<p><strong><span style="color: #0000ff;">Probable total                                                      $1200</span></strong></p>
<p><span style="color: #0000ff;">                                    - &#8211; - &#8211; - &#8211; o &#8211; o &#8211; o &#8211; o- &#8211; - &#8211; - &#8211; - </span></p>
<p style="text-align: left;"><span style="color: #0000ff;"> </span></p>
</div>
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		<title>March 2010 &#8211; Sundry Projects</title>
		<link>http://fastalley.com/2010/03/15/march-2010-sundry-projects/</link>
		<comments>http://fastalley.com/2010/03/15/march-2010-sundry-projects/#comments</comments>
		<pubDate>Tue, 16 Mar 2010 00:49:58 +0000</pubDate>
		<dc:creator>admin</dc:creator>
				<category><![CDATA[Projects]]></category>
		<category><![CDATA[Fastalley]]></category>
		<category><![CDATA[Lauren Williams]]></category>
		<category><![CDATA[trimaran]]></category>

		<guid isPermaLink="false">http://fastalley.com/?p=474</guid>
		<description><![CDATA[MARCH 2010 – SUNDRY PROJECTS Companionway Hatch Shocks Companionway Hatch Bar Heat Exchanger Bolts Replaced Kitchen Sink Re-Bedded Deck Hatch Replaced Weems &#38; Plaath clock fixed   INTRODUCTION  Let me explain that firstly I am a woman and secondly an IT Project Manager by profession, so doing boat fixes or manual labor has never been in [...]]]></description>
			<content:encoded><![CDATA[<p><strong><span style="text-decoration: underline;">MARCH 2010 – SUNDRY PROJECTS</span></strong></p>
<ul>
<li>Companionway Hatch Shocks</li>
<li>Companionway Hatch Bar</li>
<li>Heat Exchanger Bolts Replaced</li>
<li>Kitchen Sink Re-Bedded</li>
<li>Deck Hatch Replaced</li>
<li>Weems &amp; Plaath clock fixed</li>
</ul>
<p> </p>
<p><strong><span style="text-decoration: underline;">INTRODUCTION</span></strong> </p>
<p>Let me explain that firstly I am a woman and secondly an IT Project Manager by profession, so doing boat fixes or manual labor has never been in my set of skills.  The most exercise I do is running my fingers over a computer keyboard.</p>
<p> Also I have never owned any tools until I got the boat, and now I have inherited enough tools for a small workshop. </p>
<p>Since trying my hand at boat projects, I have also noticed that women obviously haven’t gone into the marine <span style="text-decoration: underline;">parts design</span> profession, because men seem to know automatically how things work – its seems so obvious to them &#8211; whereas I have to revert to reading the instructions and even then they don’t make much sense to me. </p>
<p> A Man’s mind obviously works differently to a Female’s mind.</p>
<p> I am learning on my boat that I often have to replace parts (you cannot repair them) – I think it’s a conspiracy with marine spare parts makers because just when you replace PartA then PartB caves in. </p>
<p> I also suspect that boat parts are primed to fail <span style="text-decoration: underline;">serially</span> so that you spend the entire summer working &#8211; and $spending &#8211; on the boat. </p>
<p> </p>
<p><strong><span style="text-decoration: underline;">COMPANIONWAY HATCH SHOCKS</span></strong></p>
<p> The shocks that hold the companionway hatch open suddenly decided to give up the ghost.  One moment the shocks were holding up the hatch, the next it slammed down narrowly missing my head.</p>
<p>So I examined the hatch shocks trying to figure out how to remove them so that I could take them to West Marine for replacement.  Obviously a man built the stupid part because there wasn’t any indication of how to prize the shock off its mount.  Really, if a woman had designed the piece there would have been a large arrow with engraved instructions.  All highlighted in pink.</p>
<p> Empty handed I went to West Marine, found the same part on their shelves, and spent 5 minutes examining the instructions on how to remove it – it was embarrassingly easy.  I returned to the boat, prized off the piece, returned to West Marine and bought the same (length) size.</p>
<p>The gas shock said it would hold up 90 lbs.  The instructions said if I had 2 shocks before, then I should replace with 2 again.  I realized my hatch was at most 25 lbs, so 180 lbs was a bit of overkill, but that seemed to be the only weight:length combination that would fit my hatch. So I shelled out the $50.</p>
<p>Back I went to the boat, clicked the new gas shocks into place and watched admiringly as the hatch stayed open and did not slam down on my head.  Then I tried to close the hatch.  Before, with the old shocks, I simply leaned gently on the hatch and it closed.  Now I yanked and yanked but the hatch didn’t move.  Thinking the gas shocks were somehow stuck in the “open” position I went back to the instructions to figure out how to unstuck them.  The instructions didn’t cover this.</p>
<p><img class="alignleft size-thumbnail wp-image-487" title="DSC02296" src="http://fastalley.com/wp-content/uploads/2010/03/DSC02296-300x150.jpg" alt="DSC02296" width="300" height="150" /></p>
<p>After staring at the obstinate hatch some more I realized that maybe 180lbs force to keep the hatch open, required a similar opposite force to close it.  So I grabbed the hatch, leaned my full weight on it, and down it came – reluctantly.  In fact, it took so much effort that I figured I could use the open hatch as an exercise bar for chin ups. </p>
<p>Then I tried to close the hatch from inside the cabin but I couldn’t pull hard enough to bring down the hatch, and keep it down.  Back to the drawing board.  I stared mutely at the gas shocks.  They stared back unhelpfully.</p>
<p>Eventually I removed one of the gas shocks reducing the load to 90 lbs again – notwithstanding the instructions that if I had 2 shocks then I should replace with 2 new shocks.  Bringing down the hatch against 90 lbs force is still pretty heavy for me especially when pulling it down from inside the cabin, but at least it stays open as desired. </p>
<p><strong><span style="color: #0000ff;">Price:  $25 each  &#8212;&#8212;&#8211;&gt;&gt;&gt;&gt; pleasant surprise, I only needed one.</span></strong></p>
<p> </p>
<p><strong><span style="text-decoration: underline;">COMPANIONWAY HATCH BAR</span></strong></p>
<p>When you close the companionway hatch then the crossbar or beam across the front of the hatch has part of the bar protruding out at the corner.  The screw that is supposed to keep the corner flush had worked thru the steel bar and under it, and so it was no longer lying flush.  Every time I pulled the hatch down and tried to close it, it balked at the slightly protruding piece.</p>
<p>Previously I had the protruding piece glued back in place, but with minimal continued use, pretty soon it come unstuck again.</p>
<p>This time I decided to remove the flat head (sunken) screw and get another one with a bigger head so that it could not work thru the steel.  Then glue it as well for good measure, clamp it all together, and wait. </p>
<p>Of course, having made this decision I then realized I don’t own a clamp – so it’s off to Home Depot again.</p>
<p>I used to love shopping and browsing thru malls for all manner of frilly things.  Lately my shopping habits rotate between West Marine and Home Depot.</p>
<p><strong><span style="color: #0000ff;">Cost to fix (my labor comes free):  93 cents for a bag of flat head screws</span></strong></p>
<p><strong> </strong></p>
<p><strong><span style="text-decoration: underline;">HEAT EXCHANGER BOLTS REPLACED</span></strong></p>
<p>I thought I had to change the impeller so I got a mechanic, Bill, to take a look at the engine.  He declared the impeller just fine, but when he touched the heat exchanger it came loose in his hands.  It looked like the bolts had sheared off. </p>
<p>The solenoid was also hanging loose from its mounting.</p>
<p>It seems the heat exchanger had 2 bolts – or is that screws, I never could tell the difference – anyway it was big and it had a thread.  One bolt was too big for its hole, and the other bolt too small for its hole.  To the casual gaze it all looked secure, but in fact was completely unsecured.  One bolt had sheared off and the base of the bolt was embedded in its hole.  The other bolt was so loose it came out in his hand.  It was basically just sitting loose in the hole, not actually screwed in.  I was so lucky that the whole contraption hadn’t fallen off during our trip up the coast from Long Beach which would have done irreparable damage to the engine.</p>
<p>I was bemoaning the problem to a colleague at work, telling him that the previous mechanic had put a 3/8 inch bolt in a 1/2 inch hole.  My colleague said he understood perfectly – in fact, his last girlfriend kept complaining about the same thing.  I added that when touched, the thing just fell out in my hand.  My colleague nodded – he said his ex complained about that too.  He didn’t like his ex that much, he said.  Super helpful colleague &#8211; not.</p>
<p>Bill drilled the embedded bolt base out and found the threads were gone so we couldn’t replace the bolt with a new one.  Instead he went off and created a base plate that he bolted to the engine and then bolted the heat exchanger onto its new base plate.  It looks and feels really solid now. </p>
<p><img class="alignleft size-thumbnail wp-image-488" title="DSC02311" src="http://fastalley.com/wp-content/uploads/2010/03/DSC02311-300x150.jpg" alt="DSC02311" width="300" height="150" /></p>
<p>He also bolted the solenoid to the new plate.   With all the work I have had done on the engine in the last year, I hope it lasts at least another 1000 hours before I need to rework anything again.    </p>
<p><strong><span style="color: #0000ff;"> </span></strong></p>
<p><strong><span style="color: #0000ff;"> </span></strong></p>
<p><strong><span style="color: #0000ff;"> </span></strong></p>
<p><strong><span style="color: #0000ff;">Mechanical fix:  $300 = $50 in parts and $250 mechanic’s labor.</span></strong></p>
<p> </p>
<p> </p>
<p><strong><span style="text-decoration: underline;">KITCHEN SINK RE-BEDDED</span></strong></p>
<p>The kitchen sink has small bolts underneath it, one in each corner, to hold it firmly in place.  However, the tiny bolts were obviously not effective because they had rusted off over time and the back left corner of the sink lifted out of its hole, leaving a gap between the sink and the counter.</p>
<p>For ages I worried that when I washed the dishes any splashed water on the counter would seep under the gap and drip down onto the refrigerator below.  Finally it bugged me enough that I decided to take a peek.   Sure enough, water had seeped down under the sink and worse, had dripped onto the fridge electric cabling.</p>
<p>To avoid any further damage to the underlying refrigerator, I stuck blue painters tape all around the sink until I figured out a fix.  Actually the makeshift tape worked so well, that I left it like that all winter.</p>
<p>Now that the Spring has sprung, and the grass is ris…..  its time to fix the damn thing.</p>
<p>Did some shopping at Home Depot – again.  Got the acetone, got the scraper, the painters tape, the clamps, got the DAP caulk for kitchens – time to try my hand at this new boat project.</p>
<p><img class="alignleft size-thumbnail wp-image-491" title="DSC02297" src="http://fastalley.com/wp-content/uploads/2010/03/DSC02297-300x150.jpg" alt="DSC02297" width="300" height="150" /></p>
<p>I squeezed the scraper all the way around and under the kitchen sink trying to prize it out of its hole but no luck.  It stuck firmly in the two front corners.  I fiddled around underneath and felt clamps in the two corners keeping the sink embedded.  These 2 front clamps hadn’t rusted off.  After 20 minutes of contortions trying to get the clamps unscrewed I decided the only way to reach anything under the sink was to remove the refrigerator.</p>
<p>Amazingly the fridge is held in place with just 4 smallish screws, so I unscrewed them, read the DANGER SHOCK sign on top of the fridge and hurriedly turned off the mains – and the batteries for good measure &#8211; then I dragged the fridge out of its cubbyhole.  This left a nice big gap under the sink that I could now reach into.  I removed the clamps on the 2 front corners – the back 2 having already rusted off long ago.   I could only heft the sink out about 2 inches because it was still connected underneath to its plumbing.  Try as I might I didn’t have the strength to disconnect the threaded hose, so eventually I gave up the unequal struggle.</p>
<p><img class="alignright size-thumbnail wp-image-492" title="DSC02298" src="http://fastalley.com/wp-content/uploads/2010/03/DSC02298-300x150.jpg" alt="DSC02298" width="300" height="150" /></p>
<p>I thoroughly cleaned around the sink with my new acetone, re-taped the area with the blue painters tape, cut the caulking spout at a 45 degree angle per the instructions, and squeezed the caulking under the rim.  Man, that caulking stuff is messy.  I managed to get it all over the place and especially all over my fingers.  Thank heavens for the painters tape otherwise it would have been all over the counter too. </p>
<p>After I caulked it all and left it for awhile, I noticed that I hadn’t done a very thorough job – notwithstanding the amount of caulk on my hands.  So I re-taped the sink perimeter and recaulked it again.  Second time around it seemed so much simpler.  Finally I pushed the refrigerator back into its cubby hole under the sink, screwed it back in place, cleaned up the mess, and left it to dry. </p>
<p><img class="alignright size-thumbnail wp-image-490" title="DSC02302" src="http://fastalley.com/wp-content/uploads/2010/03/DSC02302-300x150.jpg" alt="DSC02302" width="300" height="150" /></p>
<p>I decided to watch On Golden Pond while I made dinner.  A nice quiet movie I thought because after the last 4 hours I didn’t need any added stress.  Unfortunately its all about an old man with Old Timers having massive stress attacks as he gets lost and forgetful – so that didn’t help my stress levels any.</p>
<p>But the sink is looking good.  The instructions said not to use water around the caulking for 24 hours so I will check the seal next weekend by squirting water all around the rim of the sink and check that nothing drips through onto the fridge beneath.</p>
<p>(Next weekend….. the caulk is holding beautifully.  There is absolutely no water seeping thru).</p>
<p><strong><span style="color: #0000ff;">Cost of repair (my labor is free):   $8 in caulking, tape, etc.</span></strong></p>
<p> </p>
<p><strong><span style="text-decoration: underline;">DECK HATCH REPLACED</span></strong></p>
<p>Winter in San Francisco is wet, wetter, wettest with strong cold winds howling across the Bay.  Even as the weather warms, it is not much better.  In fact, Mark Twain said something like… the coldest season he ever endured was the summer he spent in SanFran.  Or words to that effect.</p>
<p>So when I finally returned to the boat after weeks of awful weather, I found rain water had dribbled in through a bunch of hatches.  At $300 per hatch, the wet patches were not a fun sight.</p>
<p>Off to West Marine where I ordered one new Bomar hatch, and picked it up a few days later.  I thought I would need a handyman to replace the hatches for me, but Bill (the local mechanic) took a look and said – you look smart enough, you can do this yourself.  He gave me a list of stuff to buy at West Marine and Home Depot, told me exactly what to do, and exited.</p>
<p>This is just like caulking the sink – just using a different kind of caulk and some brute force to tug the old hatch out of its hole.  First you have to use a sharp knife to cut around the rim of the hatch to “release” it where it has set itself over the years into its hole, then unscrew all the screws and put them together in a baggie so that you don’t lose them.  Then use a thin scraper and work it under the rim so that you break the seal where the rim is glued in place.  Use a hammer if you lack the strength to really get the scraper under the rim.  Once you have worked all the way around under the rim, give the hatch a tug.  Actually mine came out relatively easily – witness the water that had dripped into the boat – obviously the caulk wasn’t holding it in very tightly.</p>
<p>After tugging out the hatch, scrape and clean the area thoroughly using rubbing alcohol or acetone.  Maybe even sand it a little with fine 100 sandpaper to rough it up for the caulk.  Lay down a perimeter of blue painters tape so that if any of the caulk squeezes out then it will not ruin your deck.  I put down enough caulk to seal the Titanic then I dropped the new hatch into its hole and got caulking all over me and the tape as it squeezed out all over.  I quickly wiped it away with an old telephone card. </p>
<p>TIP – here is a useful tip I got from someone.  Keep old telephone cards whenever you find them.  People throw them away when they are “empty”.  The edge of the card is perfect for scraping up caulk and leaving just the right size bead in place.   Or you can use your old Gold Card that has maxed out its credit limit &#8211; that works just as well too.</p>
<p><img class="alignright size-thumbnail wp-image-495" title="DSC02310" src="http://fastalley.com/wp-content/uploads/2010/03/DSC02310-300x150.jpg" alt="DSC02310" width="300" height="150" /></p>
<p>Don’t tighten the screws down tight right away because you will squeeze out all the caulk you just carefully laid.  The weight of the hatch is enough for now.  Replace the screws lightly in their holes.  2 hours later the caulk has set up a little so you can tighten the screws a little more, and wipe away the excess that squeezes out the sides.  2 hours later tighten the screws just short of “very tight” and leave to dry for a few more hours.  Finally when you think the caulk is mostly set, tighten the screws that final little bit.  Even though it is 8 hours later and you think the caulk is firmly set, a thin line of caulk will still squeeze out – I didn’t wipe it away, I left it in place as a sealing cushion.  Maybe a man would have cleaned it up the final time, but I didn’t.  This is my first hatch that I ever replaced and with no one watching over my shoulder, and lacking experience, I just followed my (female) logic.</p>
<p><strong><span style="color: #0000ff;"><strong><span style="color: #0000ff;">Cost to fix (my labor comes free):</span></strong>  $260 for the new hatch + $8 in caulk, tape, acetone, etc</span></strong></p>
<p> </p>
<p><strong><span style="text-decoration: underline;">WEEMS &amp; PLAAT Clock</span> </strong></p>
<p>My W&amp;P clock stopped working.  My first thought was that the battery was flat.  It is a French made clock so finding a small “N” battery (1/3 the size of a AAA) was easier said than done, but eventually I found 2 so I bought them both.  I installed the new battery in the clock only to find that the clock still didn’t work.  The clock innards were at fault.  Another thing to (expensively) replace instead of (cheaper) repair.  </p>
<p>I checked the clocks in the West Marine catalog and they cost $145 – no kidding, $145 for a clock about 6 inches in diameter with no special features like say brass numerals, or fancy interior brass clock wheels, or even a cuckoo.  Just a run-of-the-mill everyday clock.</p>
<p>There are a lot of parts of the boat that are very expensive to replace but I could not bring myself to shell out $145 for an everyday clock. </p>
<p>So the chap in the next boat unscrewed the clock from the wall and turned it over and we examined it closely.  Before I had just glanced at the parts as I replaced the battery but now I took a good look.  Turns out the innards of the clock is just a little plastic box – the kind you see at the craft store <em>Michaels</em> for all those crafters that like making their own clocks.   We gently prized out the little box and examined it – yep, it was exactly like the <em>Michaels</em> clocks except for the raised letters that said “Made in France”. </p>
<p>I took the little plastic box down to the <em>Michaels</em> store to make sure I bought the same size replacement part, handed over $7 for the new piece – with new clock hands – and returned to my Weems &amp; Plaath clock.   I took the clock apart, removed the French hands (they didn’t fit the <em>Michaels</em> piece), replaced the hands with my new hands, noticed the face of the clock is just a plain ole piece of PAPER with black lettering, inserted my new easy to obtain USA battery – and voila! my clock works again.</p>
<p><img class="alignright size-thumbnail wp-image-496" title="DSC02309" src="http://fastalley.com/wp-content/uploads/2010/03/DSC02309-300x150.jpg" alt="DSC02309" width="300" height="150" /></p>
<p>So lets see….. the components of the W&amp;P clock are the expensive non-rust outer shell that screws to the wall, say $3 to manufacture each little holder.  The faceplate of the little clock is glass so lets say 50cents.  Then there is the paper clock face with black numeral lettering, lets say 2cents.  That is a total of $3.52 for the clock so far. </p>
<p>So W&amp;P reckon that the $7 part that you can buy at <em>Michaels</em> actually costs more than $140 if it says Made in France.  I know, I know, there is W&amp;P distribution and marketing costs included in the price, but <em>Michaels</em> has those same costs – so they negate each other in my book.</p>
<p>So – advice to you ladies – if your Weems &amp; Plaath clock goes on the blink, don’t pay $145 for a new one, buy the $7 replacement part and fix it yourself.</p>
<p><strong><span style="color: #0000ff;">Cost to fix (my labor comes free):  $7 in parts</span></strong></p>
<p style="text-align: center;"><strong>&lt;&lt;&lt;&lt;&lt;&lt; &#8212;&#8211; End of March projects &#8212;&#8211; &gt;&gt;&gt;&gt;&gt;&gt;&gt;</strong></p>
<p align="center"><strong> </strong></p>
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		<title>SEPT 2009 &#8211; Painting the topsides</title>
		<link>http://fastalley.com/2009/08/30/sept-2009-painting-the-topsides/</link>
		<comments>http://fastalley.com/2009/08/30/sept-2009-painting-the-topsides/#comments</comments>
		<pubDate>Mon, 31 Aug 2009 00:32:07 +0000</pubDate>
		<dc:creator>admin</dc:creator>
				<category><![CDATA[Projects]]></category>
		<category><![CDATA[Fastalley trimaran painting topsides]]></category>

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		<description><![CDATA[SEPT 2009 &#8211; Painting the topsides Bottom paint The following was included in this item. We hauled out the vessel, pressure and solvent washed the hull bottom, applied one coat of antifouling bottom paint with two coats at the water line and launched your vessel. The bottom paint was applied with rollers and brushes. NOTE [...]]]></description>
			<content:encoded><![CDATA[<p><strong>SEPT 2009 &#8211; Painting the topsides</strong></p>
<p><strong>Bottom paint</strong><br />
The following was included in this item. We hauled out the vessel, pressure and solvent washed the hull bottom, applied one coat of antifouling bottom paint with two coats at the water line and launched your vessel. The bottom paint was applied with rollers and brushes.</p>
<p>NOTE 1: The bottom paint applied is Seahawk AF-33 (black) antifouling bottom paint.</p>
<p><strong>Removal of additional marine growth, and sanding and spot priming of bare spots</strong><br />
In addition to the scope of work described above, we sanded and spot primed several bare areas on the hulls where primer was showing through the existing bottom paint. This was necessary to provide proper adhesion of the anti-fouling paint. Sanding and spot priming of<br />
bare areas was charged on a time and materials basis. We did not provide a Change Order due to the work in this section not exceeding more than the ten man-hours labor re-authorized in the original work</p>
<p><strong>Repaint the hull topsides and underneath the bridge deck</strong><br />
The vessel’s representative requested an estimated cost to repaint the hull topsides, underneath the bridge deck, and the bootstripes. We provided the vessel’s representative a verbal estimate of between $4,000.00 and $5,000.00. Later we received e-mail authorization to repaint these areas.</p>
<p>We tapped off the waterline and along the upper limit of the deck edge (approximately where the non-skid starts), and various hardware. Due to ease of removing two deck plates and four scuppers mounted on the undersides of the bridge deck, we removed them instead of tapping<br />
them off.  We began sanding the above-described areas to remove the existing paint down to a solid substrate suitable for applying primer.  We found that the layer of paint below the outer layer was a poorly cured one-part paint similar to Latex. This inner layer of paint could<br />
not be removed by normal sanding due to gumming up and burning the sand paper. We removed this layer of paint with a grinder, then sanded the areas with a soft pad to remove the swirls created by the grinder.</p>
<p>Filled and sanded flush approximately 12 small areas of dings or gouges. While performing this work, we noted a crack in the fiberglass skin on the outboard forward starboard deck edge, and cracks on the bow pulpit. We contacted the vessel’s representative regarding these<br />
cracks. The vessel’s representative viewed these cracks and elected to not have us repair them prior to painting due to time and budgetary constraints. NOTE: These cracks will allow water intrusion and rot that will affect the structural integrity of the underlying wood.</p>
<p>Sprayed the prepared areas with primer. Sanded the primer and filled several additional areas near the repairs of the hull to bridge deck joints, and on the outboard side of the starboard hull. These areas were spot primed, sanded, and then the hull topsides was painted with Awlgrip “Snow White” L.P. paint.</p>
<p>Taped off, and painted the bootstripes Awlgrip “Pearl Grey”.</p>
<p><span style="color: #0000ff;"><strong>TOTAL COST of repairs and painting =  $7,558.63</strong></span></p>
<p><span style="color: #0000ff;"><strong> </strong></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><img class="aligncenter size-medium wp-image-408" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-113-590x214.png" alt="Picture 1" width="590" height="214" /></p>
<p><img class="aligncenter size-medium wp-image-409" title="Picture 11" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-114-590x216.png" alt="Picture 11" width="590" height="216" /></p>
<p><img class="aligncenter size-medium wp-image-410" title="Picture 20" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-201-590x223.png" alt="Picture 20" width="590" height="223" /></p>
<p><img class="aligncenter size-medium wp-image-411" title="Picture 27" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-271-590x330.png" alt="Picture 27" width="590" height="330" /></p>
<p><img class="aligncenter size-medium wp-image-412" title="Picture 30" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-301-590x437.png" alt="Picture 30" width="590" height="437" /></p>
<p><img class="aligncenter size-medium wp-image-413" title="Picture 33" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-331-590x445.png" alt="Picture 33" width="590" height="445" /></p>
<p><img class="aligncenter size-medium wp-image-414" title="Picture 37" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-37-590x328.png" alt="Picture 37" width="590" height="328" /></p>
<p><img class="aligncenter size-medium wp-image-415" title="Picture 39" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-39-590x212.png" alt="Picture 39" width="590" height="212" /></p>
<p><img class="aligncenter size-medium wp-image-417" title="Picture 40" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-40-590x440.png" alt="Picture 40" width="590" height="440" /></p>
<p><img class="aligncenter size-medium wp-image-418" title="Picture 42" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-42-590x442.png" alt="Picture 42" width="590" height="442" /></p>
<p><img class="aligncenter size-medium wp-image-419" title="Picture 45" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-45-590x444.png" alt="Picture 45" width="590" height="444" /></p>
<p><img class="aligncenter size-medium wp-image-420" title="Picture 46" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-46-590x211.png" alt="Picture 46" width="590" height="211" /></p>
<p><img class="aligncenter size-medium wp-image-421" title="Picture 6" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-62-590x438.png" alt="Picture 6" width="590" height="438" /></p>
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		<title>AUG 2009 &#8211; Hull repairs</title>
		<link>http://fastalley.com/2009/08/24/aug-2009-hull-repairs/</link>
		<comments>http://fastalley.com/2009/08/24/aug-2009-hull-repairs/#comments</comments>
		<pubDate>Mon, 24 Aug 2009 23:28:40 +0000</pubDate>
		<dc:creator>admin</dc:creator>
				<category><![CDATA[Projects]]></category>
		<category><![CDATA[Fastalley]]></category>
		<category><![CDATA[hull repairs]]></category>
		<category><![CDATA[trimaran]]></category>

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		<description><![CDATA[AUG 2009 &#8211; Hull repairs While bringing the boat up from La Paz to Long Beach, we hit a set of waves that ripped the skin of the port ama.  We did a temporary glassing in MX but it was just a rush job, and not professionally done, and it was feared that water may [...]]]></description>
			<content:encoded><![CDATA[<p><strong>AUG 2009 &#8211; Hull repairs</strong></p>
<div id="attachment_404" class="wp-caption aligncenter" style="width: 600px"><img class="size-medium wp-image-404" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/08/Picture-12-590x439.png" alt="Haul out" width="590" height="439" /><p class="wp-caption-text">Haul out</p></div>
<p>While bringing the boat up from La Paz to Long Beach, we hit a set of waves that ripped the skin of the port ama.  We did a temporary glassing in MX but it was just a rush job, and not professionally done, and it was feared that water may be trapped under the glass which would cause a whole &#8216;nother set of problems.</p>
<p>It was decided to remove the quickie repair and do it again professionally in Long Beach.  At the same time we would structurally reinforce the hulls so that it was much stronger.</p>
<p>Copied from the invoice of the boatworks that did the work&#8230;&#8230;</p>
<p><strong>Hull repairs</strong><br />
Upon the vessel’s arrival and prior to haulout, we visibly inspected the reported areas of the hull damage in an effort to determine if the vessel was structurally sound enough for hauling out with only slings.   After haulout, we further evaluated the condition of reported areas of damage, and reviewed the owner-supplied construction drawings.   We found that there was a fillet in the areas of cracking.  This fillet had no structural fibers in it, and the fillet was excessively large.  Over time, this non-reinforced fillet had cracked.  Upon grinding out the cracking fillet, we noted cracking in the underlying fiberglass skin.</p>
<p>We conferred with a Naval Architect regarding the cracking who requested that we grind out the failed fillet so that the underlying fiberglass skin could be viewed. We ground out the failed epoxy fillet and noted cracks in the underlying fiberglass skin, but did <span style="text-decoration: underline;">not</span> note any visible evidence of wood rot, or structural failure.</p>
<p>As recommended by the Naval Architect, we ground off the surrounding fiberglass skin approximately 4” – 5” outwards from the junction of the hulls to bridge deck, and also sanded off the paint outboard of the removed fiberglass skin approximately 2” – 3&#8243; so that we could get good continuity between the wood, the existing fiberglass skin and the new fiberglass laminates that are applied using WEST system epoxy.  WEST system bonds very well to wood and the old fiberglass skin.</p>
<p>Installed a properly sized epoxy fillet that is reinforced with micro-fibers. Applied two layers of DBM fiberglass roving @ +/- 45 degrees over the junctions of the hulls to the underside of the bridge deck, using West System. The areas were sanded, primed, epoxy filled, and moderately faired.</p>
<p>(Owner comment:  After viewing the repairs, the Naval Architect said the boat&#8217;s life had been extended 15 years at least).</p>
<p> </p>
<p>Labor &#8230;&#8230;&#8230;&#8230;&#8230;&#8230;. $7,540.00<br />
Proj. Mgmt. &#8230;&#8230;&#8230; $754.00<br />
Consumables&#8230;&#8230;. $829.40<br />
Supplies &#8230;&#8230;&#8230;&#8230;.. $2,212.06<br />
<span style="color: #0000ff;"><strong>Section total  =  $11,335.46</strong></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><strong>Replace propshaft zinc</strong><br />
Upon the vessel’s arrival and haulout, we noted that the propshaft zinc<br />
was extremely deteriorated and close to falling off. We removed the<br />
propshaft zinc, cleaned the mounting location of the zinc to remove<br />
surface corrosion, purchased and installed a new zinc.<br />
<strong><span style="color: #0000ff;">No Charge</span></strong></p>
<p><strong><span style="color: #0000ff;"> </span></strong></p>
<p><strong><span style="color: #0000ff;"> </span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-370" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-111-590x437.png" alt="Picture 1" width="590" height="437" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-371" title="Picture 3" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-36-590x215.png" alt="Picture 3" width="590" height="215" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-372" title="Picture 4" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-41-590x440.png" alt="Picture 4" width="590" height="440" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-373" title="Picture 5" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-51-590x218.png" alt="Picture 5" width="590" height="218" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><br />
<img class="aligncenter size-medium wp-image-374" title="Picture 6" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-61-590x438.png" alt="Picture 6" width="590" height="438" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-375" title="Picture 7" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-71-590x216.png" alt="Picture 7" width="590" height="216" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-376" title="Picture 8" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-81-590x441.png" alt="Picture 8" width="590" height="441" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-377" title="Picture 9" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-91-590x215.png" alt="Picture 9" width="590" height="215" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-378" title="Picture 10" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-101-590x216.png" alt="Picture 10" width="590" height="216" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-379" title="Picture 11" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-112-590x438.png" alt="Picture 11" width="590" height="438" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-380" title="Picture 12" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-121-590x215.png" alt="Picture 12" width="590" height="215" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-381" title="Picture 13" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-132-590x438.png" alt="Picture 13" width="590" height="438" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-382" title="Picture 14" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-141-590x439.png" alt="Picture 14" width="590" height="439" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-383" title="Picture 15" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-151-590x220.png" alt="Picture 15" width="590" height="220" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-384" title="Picture 16" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-161-590x215.png" alt="Picture 16" width="590" height="215" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-385" title="Picture 17" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-171-590x427.png" alt="Picture 17" width="590" height="427" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-386" title="Picture 18" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-181-590x438.png" alt="Picture 18" width="590" height="438" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-382" title="Picture 14" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-141-590x439.png" alt="Picture 14" width="590" height="439" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-383" title="Picture 15" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-151-590x220.png" alt="Picture 15" width="590" height="220" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-384" title="Picture 16" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-161-590x215.png" alt="Picture 16" width="590" height="215" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-385" title="Picture 17" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-171-590x427.png" alt="Picture 17" width="590" height="427" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-386" title="Picture 18" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-181-590x438.png" alt="Picture 18" width="590" height="438" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-387" title="Picture 19" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-191-590x213.png" alt="Picture 19" width="590" height="213" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-389" title="Picture 21" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-211-590x452.png" alt="Picture 21" width="590" height="452" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-390" title="Picture 22" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-221-590x216.png" alt="Picture 22" width="590" height="216" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-391" title="Picture 23" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-231-590x443.png" alt="Picture 23" width="590" height="443" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><img class="aligncenter size-medium wp-image-392" title="Picture 24" src="http://fastalley.com/wp-content/uploads/2009/12/Picture-241-590x212.png" alt="Picture 24" width="590" height="212" /></span></strong></p>
<p><strong><span style="color: #0000ff;"><br />
</span></strong></p>
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		<title>AUG 2009 &#8211; Mechanical and Electrical work</title>
		<link>http://fastalley.com/2009/08/23/aug-2009-mechanical-and-electrical-work/</link>
		<comments>http://fastalley.com/2009/08/23/aug-2009-mechanical-and-electrical-work/#comments</comments>
		<pubDate>Sun, 23 Aug 2009 23:10:42 +0000</pubDate>
		<dc:creator>admin</dc:creator>
				<category><![CDATA[Projects]]></category>
		<category><![CDATA[electrical]]></category>
		<category><![CDATA[Fastalley]]></category>
		<category><![CDATA[mechanical]]></category>
		<category><![CDATA[repairs]]></category>
		<category><![CDATA[trimaran]]></category>

		<guid isPermaLink="false">http://fastalley.com/?p=351</guid>
		<description><![CDATA[Aug 2009 &#8211; Mechanical and electrical work This work was done professionally at a boatyard &#8211; and copied from their invoice. Upon the vessel’s arrival and haulout, we evaluated the vessel’s charging systems to include the battery condition, battery charger, wind generator, and solar panels. We found that one of the Gel-cell house batteries was [...]]]></description>
			<content:encoded><![CDATA[<p><strong>Aug 2009 &#8211; Mechanical and electrical work</strong></p>
<p>This work was done professionally at a boatyard &#8211; and copied from their invoice.</p>
<p>Upon the vessel’s arrival and haulout, we evaluated the vessel’s charging systems to include the battery condition, battery charger, wind generator, and solar panels.</p>
<p>We found that one of the Gel-cell house batteries was bad and would not hold a charge. The vessel’s representative for the owner informed us that he would replace the battery himself at a later date.  (The cost to replace all 4 house batteries is around $1000).<br />
It was also found that the battery charger was charging the start battery, but was not charging the house bank. We troubleshot the battery charger and found that the leads to the house bank had no output.  Due to the battery charger having two outputs, we connected the working output to the house bank, and took the dead battery out of the house bank.  We found that the battery charger was capable of charging the house bank with the one working output. We returned the charger wiring back to its original configuration. We recommend that the vessel owner purchase and install a new battery charger.<br />
When we had adequate wind conditions, we checked the output of the wind generator, and the stop function. We found the output of the wind generator to fluctuate with the wind speed, and when placed in “stop” mode, the generator blades slowed as per the manufacturer’s literature.<br />
We checked the output of the solar panels and found that it had no output. No other work was performed on the solar panel.<br />
Upon the vessel’s arrival (at the boatyard), we inspected the hose that was contacting a drive belt, and alternator adjustment limitation. We found that at some time in the past a larger alternator had been installed. With the larger alternator, there was not adequate adjustment room for the alternator without the alternator case contacting the stud on the motor mount. In addition, the raw water hose was routed close to the alternator drive belt where the loose drive belt was wearing away the hose. We contacted the vessel’s representative regarding the limited adjustment clearance.  The vessel’s representative authorized cutting the stud of<br />
the motor mount shorter to provide additional clearance. As authorized by the vessel’s representative, we cut down the excess stud above the lock nuts on the motor mount and were able to adjust the alternator drive belt tension. We removed the worn raw water hose. Purchased a new length of raw water hose, bronze hose barbs, and a bronze 90 degree elbow. Installed the new hose and bronze fittings so that the plumbing is routed away from the drive belt.</p>
<p>We checked the vessel’s forward bilge pump by activating the manual toggle switch and listening for the bilge pump’s motor. We also checked the float switch in the forward bilge by lifting the float switch and listening for the bilge pump motor. We noted that there is no float</p>
<p>switch on the aft bilge pump, but could hear the motor when the toggle switch was placed in the “manual” position. Though we could hear the motors running, we did not put water in the bilges to check if water activated the bilge pump or if the bilge pumps evacuate water.<br />
NOTE: WE highly recommend that the vessel owner test the bilge pumps by placing water in the bilge and verifying that they actually evacuate the water and there are no leaks.  (Owner&#8217;s Note:  I checked the bilge pump with water in the bilge and it pumped the engine room dry).</p>
<p>Labor       &#8230;&#8230;&#8230;&#8230;&#8230;  $373.75<br />
Proj. Mgmt&#8230;&#8230;&#8230;&#8230;.  $ 37.88<br />
Consumables&#8230;&#8230;&#8230;   $ 41.11<br />
Materials &#8230;&#8230;&#8230;&#8230;&#8230;  $43.16<br />
Supplies &#8230;&#8230;&#8230;&#8230;&#8230;.   $41.52<br />
<span style="color: #0000ff;"><strong>Section total&#8230;&#8230;. $536.92</strong></span></p>
<p> </p>
<p> </p>
<div id="attachment_365" class="wp-caption aligncenter" style="width: 600px"><img class="size-medium wp-image-365" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/08/Picture-11-590x458.png" alt="Mechanical repairs" width="590" height="458" /><p class="wp-caption-text">Mechanical repairs</p></div>
<div id="attachment_367" class="wp-caption aligncenter" style="width: 600px"><img class="size-medium wp-image-367" title="Picture 4" src="http://fastalley.com/wp-content/uploads/2009/08/Picture-4-590x216.png" alt="Mechanical repairs" width="590" height="216" /><p class="wp-caption-text">Mechanical repairs</p></div>
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		<title>JUNE 2009 &#8211; Rigging recalibrated</title>
		<link>http://fastalley.com/2009/06/13/june-2009-rigging-recalibrated/</link>
		<comments>http://fastalley.com/2009/06/13/june-2009-rigging-recalibrated/#comments</comments>
		<pubDate>Sat, 13 Jun 2009 21:40:29 +0000</pubDate>
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				<category><![CDATA[Projects]]></category>
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		<category><![CDATA[rigging recalibrated]]></category>
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		<guid isPermaLink="false">http://fastalley.com/?p=335</guid>
		<description><![CDATA[JUNE 2009 &#8211; Rigging recalibrated Even though I had had the boat for 18 months I had never sailed it.  I always seemed to be going somewhere directly upwind so that it is impossible to sail, and I usually have a tight timeline so I dont have the time to tack back and forth up [...]]]></description>
			<content:encoded><![CDATA[<p><strong>JUNE 2009 &#8211; Rigging recalibrated</strong></p>
<p>Even though I had had the boat for 18 months I had never sailed it.  I always seemed to be going somewhere directly upwind so that it is impossible to sail, and I usually have a tight timeline so I dont have the time to tack back and forth up the coast.</p>
<p>However, the primary reason reason that I had not sailed the boat is because</p>
<p>(a)  the rigging was very loose and needed calibrating</p>
<p>(b)  the main halyard had issues; it was wire and breaking down</p>
<p>(c)  the main sheet was a very thick line and barely made it through the clutch, consequently if for any reason I wanted to throw off the mainsheet &#8211; it would not run.  So the main would stick in the clutch with perhaps disasterous consequences for the boat.</p>
<p>(d) the main channel is offset about 6 ft from the top of the mast, so the main wont go all the way to the top.</p>
<p>So finally I decided it was time to fix the rigging so that I could learn to sail my boat &#8211; finally.</p>
<p>The rigger is an avid racer, and cost conservative, so he put in some innovative solutions that would work well while also saving me money.</p>
<p><strong>The following was done to the rigging:</strong></p>
<p>1)  Shortened the backstay pendant from the mast head to the tri fitting that splits the BS to each of the aft amas&#8217; chain plates to allow enough take-up to be able to tighten back stay.</p>
<p>2).  Replaced the failing wire main halyard with all rope</p>
<p>3).  Freed up the rusted sheeve at the mast head so it would spin.</p>
<p>4).  Replaced the main sheet so that it would be long enough to allow full deployment of the boom and to a smaller diameter line so that it would run better/freer thru the clutch.</p>
<p>5).  The standing rigging was tensioned to correct the rake of the mast.</p>
<p><span style="color: #0000ff;"><strong>Total Cost = $750</strong></span></p>
<p><span style="color: #0000ff;"><strong><br />
</strong></span></p>
<p><img src="file:///Users/juliabrown/Desktop/Picture%205.png" alt="" /><img class="aligncenter size-full wp-image-431" title="Picture 5" src="http://fastalley.com/wp-content/uploads/2009/06/Picture-5.png" alt="Picture 5" width="348" height="465" /></p>
<p><img class="aligncenter size-full wp-image-432" title="Picture 4" src="http://fastalley.com/wp-content/uploads/2009/06/Picture-4.png" alt="Picture 4" width="354" height="234" /></p>
<p><span style="color: #0000ff;"><strong><br />
</strong></span></p>
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		<title>MAY 2008 &#8211; Windlass overhauled</title>
		<link>http://fastalley.com/2009/05/13/may-2008-windlass-overhauled/</link>
		<comments>http://fastalley.com/2009/05/13/may-2008-windlass-overhauled/#comments</comments>
		<pubDate>Wed, 13 May 2009 21:56:02 +0000</pubDate>
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				<category><![CDATA[Projects]]></category>

		<guid isPermaLink="false">http://fastalley.com/?p=338</guid>
		<description><![CDATA[MAY 2008 &#8211; Windlass overhauled I wanted to spend a weekend anchored at White&#8217;s Island in Long Beach harbor &#8211; just for the fun of it.  This would be the first time I had anchored anywhere and I was keen to try it. A sailing friend and I put together a list of things to [...]]]></description>
			<content:encoded><![CDATA[<p><strong>MAY 2008 &#8211; Windlass overhauled</strong></p>
<p>I wanted to spend a weekend anchored at White&#8217;s Island in Long Beach harbor &#8211; just for the fun of it.  This would be the first time I had anchored anywhere and I was keen to try it.</p>
<p>A sailing friend and I put together a list of things to check before venturing out, and number 1 on the list was to check the anchoring equipment.</p>
<p>While still tied up at the dock we released and dropped the anchor off the bow.  It disappeared into the mud below.</p>
<p><strong>The Chain</strong></p>
<p>We found that there were no markings on the chain to indicate how many feet of chain had been dropped, which didnt help.  So I bought little colored anchor markers that fit between the links.  DO NOT BOTHER with these.  They are so innocuous that the anchor line runs out and the little markers pass by virtually unnoticed.  You have to be paying full attention to the chain &#8211; instead of the anchoring spot &#8211; to see the little markers in the links.  They are useless.  And they fall out of the links &#8211; contrary to the claim on the website that says they never do!</p>
<p>Eventually I abandoned the unequal battle and bought 3 cans of paint &#8211; red, white, and blue &#8211; and sprayed the chain every 25ft with a different color to indicate the length of chain payed out.   The broad paint stripes on the chain made it so much easier to see how much chain is over the side.</p>
<p>Spray painting the chain was easy &#8211; with no mess!  We picked a calm day with almost no wind and laid out the full length of the chain on the dock.  Then we marked every 25ft and pooled the chain for about 3 feet either side of the &#8220;25ft-mark&#8221; and stuffed the pool of chain into a sturdy garbage bag.  Then we sprayed the chain inside the plastic bag &#8211; so there was no mess on the dock, and no overspray onto the boat.  We did that every 25ft &#8211; I didnt care if it was super accurate, I just needed the visual confirmation of how many feet (approximately) were out, and how much chain I still had to drop.</p>
<p>We left the paint to dry which it did in an hour or two, then we rotated the chain inside the plastic bag to reveal the undersides that we hadnt/couldnt reach.  The painted chain does not stick to the plastic so it is a pretty easy exercise.  Then we resprayed the unpainted undersides of the chain and left to dry.  We repeated this a few time, just to get good coverage and by the end of the day we had brightly painted chain!  And we simply threw the plastic bags away &#8211; so no mess, no fuss.</p>
<p><strong>The windlass</strong></p>
<p>The windlass hauled up the anchor once and the second time it gave up the ghost.   We had to pull up the anchor by hand and shove ithe chain down into the hold &#8211; too manual, heavy work, not fun!</p>
<p>It was time to do some maintainance.  We manhandled the windlass off its base and my friend opened it up.  The inner workings were a mess &#8211; the &#8220;bicycle chain&#8221; that looped around the gears was broken, some pieces holding the inner links had snapped, and it was covered in rust.  It had obviously not been oiled in many years.</p>
<p>My friend &#8211; who knows stuff &#8211; broke it down into its component parts and bought new bits and pieces to replace the broken parts.  Then he put it all together again, greased the relevant parts, filled it with oil, and we manhandled it back onto its base, where we sealed it back down again.</p>
<p>Now it works effortlessly.  Just perfectly.  There is nothing like a beautifully maintained windlass to make life easier &#8230;.. (well, except maybe an electric windlass).</p>
<p><span style="color: #0000ff;"><strong>TOTAL COST = $20   &#8230;..excluding all the labor obviously!</strong></span></p>
<p><span style="color: #0000ff;"><strong><img class="aligncenter size-full wp-image-434" title="Picture 3" src="http://fastalley.com/wp-content/uploads/2009/05/Picture-3.png" alt="Picture 3" width="354" height="260" /></strong></span></p>
<p><span style="color: #0000ff;"><strong><img class="aligncenter size-full wp-image-435" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/05/Picture-1.png" alt="Picture 1" width="363" height="263" /><br />
</strong></span></p>
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		<title>JAN 2009 &#8211; New tranny &amp; engine overhaul</title>
		<link>http://fastalley.com/2009/01/13/jan-2009-new-transmission-major-engine-overhaul/</link>
		<comments>http://fastalley.com/2009/01/13/jan-2009-new-transmission-major-engine-overhaul/#comments</comments>
		<pubDate>Tue, 13 Jan 2009 20:18:02 +0000</pubDate>
		<dc:creator>admin</dc:creator>
				<category><![CDATA[Projects]]></category>

		<guid isPermaLink="false">http://fastalley.com/?p=322</guid>
		<description><![CDATA[Jan 2009 &#8211; New transmission, major engine overhaul The transmission had failed in Ensenada and had a temporary (borrowed) transmission that needed to be replaced with the new transmission. Since the engine had to be removed to get at the transmission, it was decided to do a major overhaul on the engine at the same [...]]]></description>
			<content:encoded><![CDATA[<p><strong>Jan 2009 &#8211; New transmission, major engine overhaul</strong></p>
<p>The transmission had failed in Ensenada and had a temporary (borrowed) transmission that needed to be replaced with the new transmission. Since the engine had to be removed to get at the transmission, it was decided to do a major overhaul on the engine at the same time.</p>
<p>The 40 hp Yanmar engine had 1200 hours on it at the time.</p>
<p><img class="aligncenter size-full wp-image-499" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/01/Picture-1.png" alt="Picture 1" width="427" height="439" /></p>
<p><strong>The following list was done to the engine / transmission:</strong></p>
<ol>
<li>The engine was hauled out and completely stripped down for a major overhaul.</li>
<li>Engine painted a uniform brown.</li>
<li>New transmission</li>
<li>New transmission oil cooler</li>
<li>New transmission oil cooler lines</li>
<li>New fuel filter</li>
<li>Water pump &#8211; new bearings, new cam, new power seals, new shaft</li>
<li>New alternator belt and pump</li>
<li>New raw water belt</li>
<li>Alternator, new 105 amp</li>
<li>New oil pressure sender</li>
<li>Calibrated the gauges</li>
<li>New temperature sender, and calibrated</li>
<li>New oil sender, and calibrated</li>
<li>New alarm sender</li>
<li>New wiring</li>
<li>New bilge pump for the engine room</li>
<li>New engine alarm system for temperature and oil</li>
<li>New solanoid for the glow plug</li>
<li>Separate glow plug with starter switch</li>
<li>All new hoses</li>
<li>New clamps</li>
<li>New oil filters</li>
<li>New fuel filters</li>
<li>New shaft saver coupling</li>
<li>New motor mount bolt</li>
<li>New lags and stringers (stainless steel)</li>
<li>New heat exchanger</li>
<li>New zinc</li>
<li>New tachometer</li>
<li>New volt meter</li>
<li>New gaskets &#8211; full top set,</li>
<li>New gear shift cable</li>
</ol>
<p><span style="color: #0000ff;"> </span><span style="color: #0000ff;"><strong>COST OF NEW &amp; OVERHAUL PARTS:   $6,900</strong></span></p>
<p><span style="color: #0000ff;"><img class="alignleft size-thumbnail wp-image-499" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/01/Picture-1-300x150.png" alt="Picture 1" width="300" height="150" /></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"><img class="alignleft size-thumbnail wp-image-503" title="Picture 9" src="http://fastalley.com/wp-content/uploads/2009/01/Picture-9-300x150.png" alt="Picture 9" width="300" height="150" /></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"><img class="alignleft size-thumbnail wp-image-502" title="Picture 7" src="http://fastalley.com/wp-content/uploads/2009/01/Picture-7-284x150.png" alt="Picture 7" width="284" height="150" /></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"><img class="alignleft size-thumbnail wp-image-501" title="Picture 6" src="http://fastalley.com/wp-content/uploads/2009/01/Picture-6-289x150.png" alt="Picture 6" width="289" height="150" /></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"><img class="alignleft size-thumbnail wp-image-498" title="Picture 10" src="http://fastalley.com/wp-content/uploads/2009/01/Picture-10-300x150.png" alt="Picture 10" width="300" height="150" /></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"> </span></p>
<p><span style="color: #0000ff;"><img class="alignleft size-thumbnail wp-image-499" title="Picture 1" src="http://fastalley.com/wp-content/uploads/2009/01/Picture-1-300x150.png" alt="Picture 1" width="300" height="150" /></span></p>
<p><span style="color: #0000ff;"> </span></p>
<p> </p>
<p><span style="color: #0000ff;"> </span></p>
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		<title>AUG 2008 &#8211; PAINTING THE DECK</title>
		<link>http://fastalley.com/2008/08/13/aug-2008-painting-the-deck/</link>
		<comments>http://fastalley.com/2008/08/13/aug-2008-painting-the-deck/#comments</comments>
		<pubDate>Wed, 13 Aug 2008 20:07:17 +0000</pubDate>
		<dc:creator>admin</dc:creator>
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		<guid isPermaLink="false">http://fastalley.com/?p=314</guid>
		<description><![CDATA[PAINTING THE DECK &#8211; all 800 sqft When I bought the boat in Jan 2008 the owner said that he had prepped the deck for a paint job, but had not gotten around to doing it. Besides the bad paint job (due to the prepping?) there were also (I thought) two small patches on the [...]]]></description>
			<content:encoded><![CDATA[<p><strong> </strong></p>
<p><strong>PAINTING THE DECK &#8211; all 800 sqft</strong></p>
<div id="attachment_316" class="wp-caption aligncenter" style="width: 600px"><img class="size-medium wp-image-316" title="DSC02282" src="http://fastalley.com/wp-content/uploads/2009/12/DSC02282-590x442.jpg" alt="Lots of prep work with all the stainless steel" width="590" height="442" /><p class="wp-caption-text">Lots of prep work with all the stainless steel</p></div>
<p>When I bought the boat in Jan 2008 the owner said that he had prepped the deck for a paint job, but had not gotten around to doing it.</p>
<p>Besides the bad paint job (due to the prepping?) there were also (I thought) two small patches on the deck that I wanted re-glassed.</p>
<p>Also the deck did not have any non-slip and I had found that walking around on the wet deck when at sea had to be done carefully.</p>
<p>So in August 2008 I went ahead with the new paint job.</p>
<p><strong>I did the following:</strong></p>
<p>(a)  put down the non-slip</p>
<p>(b)  re-glassed the two thin patches</p>
<p>(c)  pulled out the 2 lazarettes in front where the marine surveyor said the glass showed moisture, and re-set them</p>
<p>(d) repainted the 41 x 22 ft deck</p>
<p><span style="color: #0000ff;"><strong>COST  $9,500</strong></span></p>
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